Solutions
Clean Air Engineering's experience stretches
across a variety of industries concerned with Air Quality Management.
Sure, we do stack-testing, compliance audits and equipment
rental-- this is standard environmental compliance fieldwork,
and our testing
services are highly respected in the emissions monitoring
business.
Where Clean Air Engineering really shines
is in our ability to troubleshoot systems from raw material input to product
output-- our process engineers, many of them also field technicians, are
expert problem solvers. Since our founding in 1972, there have been few
process problems our technical staff hasn't solved.
Clean Air consulting
services balance our field services by providing
a "long-view" of processes and facility operations. Take a
look at some of the industries we work with, and see the solutions
Clean Air Engineering field technicians and engineers developed
to meet customer needs.
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Cement
Production:
Problem:
A client wanted to monitor the
HCl emissions from a cement kiln continuously for a 30 day
period. Because this was a short-term monitoring project,
the facility as a cost savings measure wanted to rent a system
to minimize equipment and labor costs.
Solution:
Clean Air Engineering was contracted
to design and install a temporary HCl CEMS utilizing gas filter
correlation (GFC) and associated data acquisition system to
meet the monitoring requirements. As part of the contract,
Clean Air provided on-site technicians to install and provide
operator training.
Innovation:
Clean Air Engineering, in conjunction
with Argonne National Laboratories, conducted an experimental
program to evaluate the feasibility of using an FTIR system
to measure HAPs at a cement kiln. The target analytes for
the program included inorganic compounds and both volatile
and semivolatile organic compounds. Specifically, the following
compounds were measured:
- hydrogen
chloride
- acetaldehyde
- benzene
- chlorobenzene
- ethylene
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formaldehyde
hexane
methylene
chloridenaphthalene
phenol
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styrene
toluene
meta-xylene
ortho-xylene
para-xylene
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All of these compounds except
ethylene are listed as HAPs by the EPA. Ethylene was included
in the program because it has been identified in cement kiln
emissions and it has the potential to form polynuclear aromatic
hydrocarbons(PAHs) under certain conditions.
In addition to the primary target
compounds listed above, ammonia (NH3), carbon dioxide
(CO2), carbon monoxide (CO), methane (CH4)
and water vapor were also measured during the program. These
compounds were included because they are known spectral interferents
in the FTIR measurement of many of the target compounds, and
all are present in cement kiln emissions.
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Electronics
Manufacturing:
Problem:
Clean Air Engineering was contracted
by an electronic circuit board manufacturer to perform an
engineering study to control VOC emissions from an uncontrolled
treater and to eliminate the need for internal offset emissions
which limited the facilityÖs production. The primary objective
was to develop a plan that would control emissions with existing
plant equipment, yet not affect the availability of four other
treaters on site.
Secondary objectives were to:
- Improve treater area ventilation;
- Verify existing equipment
operation;
- Improve operating efficiency
and reduce cost of existing thermal oxidizers.
Solution:
After evaluation of the existing
air pollution control systems, a decision was made to duct
the uncontrolled treater emissions to the two existing thermal
oxidizers. The system was designed to duct the uncontrolled
treater flow to both existing oxidizers and regulate the flow
to each oxidizer based on system load. Clean Air provided
the structural (ductwork) and engineering contol design, and
valve control logic with tie in to the existing PLC. Complete
drawings and construction plan were provided to the clientÖs
mechanical contractor, as well as on site project management
and supervision.
Result:
Once all the modifications were
completed a regulatory compliance test was performed that
demonstrated a 98% destruction efficiency and a reduction
of 16 tons/year of facility VOC emissions.
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Electrical
Utilities:
Problem:
Following a major outage that
included a precipitator rebuild, a utility client began experiencing
sparking and low power in their precipitator that appeared
to be caused by a high resistivity problem. As a potential
remedy the client switched to a different coal with no improvements
in operation. The fuels used were both low sulfur eastern
coals with moderate amounts (greater than 10%) of iron in
the ash.
Solution:
On first examination, the fuels
being used should have had low to moderate resistivity values
at the temperature of operation (about 300°F). Even with
the low sulfur content, the moderate amounts of iron present
in the ash would normally allow resistivity conditioning with
natural sulfuric acid vapor present in the flue gas. This
was shown to be the case both when modeling and measuring
the dust resistivity in the laboratory. Yet, the precipitator
was still acting as if a high resistivity dust layer were
present.
In order to verify the precipitator
readings, a coupon (six inches by six inches) was removed
from one of the collector plates. Resistivity was then determined
for the dust layer that had been clinging to the plate coupon.
It turns out that a very high resistivity dust layer that
could not be rapped or scraped off the newly installed plates
had formed. We then contacted the client to find out what
might cause such a layer.
Through further investigations
and conversations with the client, we found out that in the
past corrosion had been a problem with the precipitator. In
order to stem any future problems, the new plates had been
coated with a wax based corrosion inhibitor during the rebuild.
It was determined that during
start-up, that wax based corrosion inhibitor had somewhat
melted and coated the first layer of ash particles being collected.
Further heating to full load conditions had left a waxy coated
particle interface layer on the plates. The wax coating kept
the ash from adsorbing and reacting with moisture and/or sulfuric
acid vapor and therefore had a very high resistivity. Thus,
the precipitator readings were verified. As ash layers in
a precipitator will act like resistors in series, the highest
resistance is the one that the power will have to overcome.
The coated ash layer was also
looked at in a cross-sectional photo-micrograph taken using
a scanning electron microscope.
Result:
Clean Air Engineering recommended
that the precipitator be cleaned to remove the ash build-up
off the plates and to start-up the unit on natural gas to
drive off the volatiles of the wax based corrosion inhibitor,
before switching back to coal. As a result of these recommendations,
the precipitator power levels and resistivity returned to
normal.
Problem #2:
A large utility client had been
experiencing a nuisance opacity problem while burning high
sulfur coal. The client was burning 4% sulfur coal in cyclone
fired boilers. Pollution control equipment included an oversized
electrostatic precipitator (ESP) and three limestone absorber
modules. Ammonia injection was used upstream of the ESP to
reduce SO3 emissions. Opacity monitors placed upstream
of the absorbers showed less than 5% opacity in the flue.
However, complaints had been received from the surrounding
community regarding the stackÖs lingering plume.
Solution
Clean Air Engineering conducted
an investigative test program that was devised to determine
the cause of the plume. The study was performed using various
ammonia injection rates. The main objectives of the study
were to:
- Determine the cause of
the plume exiting the stack; and
- Determine the effects
of ammonia injection on the plume and ESP operation.
The test program included monitoring
the following parameters at the ESP inlet, outlet and at the
stack:
- SO2 and SO3
concentrations
- Particulate grain loadings
- Particle size distribution
- Particle morphology and
composition with respect to particle size
- NO and NO2
emissions
- In-situ resistivity (ESP
inlet only)
- Stack opacity by visual
emissions readings
In addition, both the inlet particulate
catches and ESP hopper samples were acquired for laboratory
resistivity measurements.
Result:
From the above work, it was
determined that the plume problem had two main sources. The
first was an abundance of sulfuric acid vapor created in the
boiler. From the test parameters, a curve was generated which
minimized SO3 emissions while maximizing ESP collection
efficiency. The second portion of the plume came from emissions
of NO2 (NOx). The client decided to
pursue methods of reducing the amount of NOx created
in the boiler.
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Metal
Refining and Processing
Problem:
An integrated steel producer
in the Midwest was faced with a challenge to continuously
monitor hydrocarbon emissions from a sinter plant scrubber
stack in response to regional ozone regulations that require
the continuous emissions monitoring of VOCs. The monitoring
application would require sampling and analysis of a saturated
gas stream. The client wanted to evaluate existing technology
for the design and purchase of a system.
Solution:
Clean Air Engineering conducted
a three month study that included the design, installation,
and operation of a temporary CEMS that was used to evaluate
three separate monitoring technologies. Data from this study
was used in the development of a monitoring plan and design
of a CEMS.
Result:
Data from this study was used
in the development of a monitoring plan and design of a CEMS.
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Mining
and Mineral Processing
Problem:
An industrial client was exceeding
the regulatory permitted particulate and opacity emission
limits for a taconite grate kiln scrubber. From the analysis
of previous emission test data, Clean Air Engineering determined
that scrubbing water carryover was significantly contributing
to measured particulate emissions, and creating an opacity
problem as well. We proposed a mist eliminator retrofit to
solve this problem.
Solution:
The Clean Air design, using
proprietary profiles and custom drainage-supports, eliminated
essentially all of the free water from the scrubber exhaust.
Clean Air Engineering designed, fabricated and supervised
the installation of the mist eliminator to fit within the
existing scrubber shell. This required the design and fabrication
of a new vane profile to meet the requirements of the systemÖs
gas flow (>600,000 acfm).
Result:
Post retrofit testing was performed
by the client and the measured particulate emissions are less
than half of the levels measured prior to the mist eliminator
retrofit. In addition to bringing the facility within its
particulate and opacity limits, the retrofit is also expected
to improve on scrubber water utilization and reduce the facilityÖs
maintenance costs.
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Plastics
Manufacturing -- Thermal
Oxidizer Optimization
A large laminate
production facility contracted Clean Air Engineering for
help in lowering the energy use of several thermal oxidizers
at its Indiana facility.
First, the Clean
Air Engineering team examined the thermal oxidizer system.
It discovered that the thermocouple that regulated fuel
flow to the oxidizer combustion chamber was placed too close
to the burner flame. Using an assortment of VOC monitors
and EPA test methods, Clean Air Engineering found that moving
the thermocouple away from the flame increased the oxidizer
efficiency by 2%. This increased efficiency, along with
other process adjustments, allowed the facility to lower
the operating temperature of it's TO from 1400° to
1300° .
Lowering the
operating temperature reduces fuel costs and increases the
life expectancy of TO components. (Estimation of propane
use $5/BTU - 5 day week) Our client will save approximately
$24,692/year.
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Surface
Coating
Clean Air Engineering has performed
numerous engineering projects, in conjunction with normal
/ routine process and oxidizer compliance demonstrations,
to optimize the operation of thermal oxidizers and to reduce
energy consumption.
As a result of these programs,
our clients have realized reduced energy usage and associated
costs, reduced CO2 (greenhouse) emissions, longer
equipment/systems life (i.e. lower temperatures reduce stress
on metallic heat exchangers), and reduced maintenance costs
for facilities.
Clean Air Engineering has determined
for one client, that the average reduction in temperature
which could be achieved through optimization of existing thermal
oxidizers has been conservatively estimated at 25°F per
TO. At that rate, the client estimated that the on-going energy
savings would total approximately $500,000 per year.
These estimated optimization
savings are for energy use reductions only. They do not include
the savings that will be realized from the elimination of
unplanned process shutdowns, lower maintenance and equipment
replacement costs, and the avoidance of damages to expensive
control and process equipment.
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Waste Treatment and Disposal
Clean Air Engineering is a strategic
supplier to a major waste-to-energy company providing compliance
testing services for six facilities. As part of the contract,
Clean Air Engineering provides quarterly, semi-annual, and
annual testing services to demonstrate compliance with regulatory
emissions limits for 19 combustor units.
The test parameters
include the determination of the following:
-
Particulate/Pm10
- Sulfur
dioxide
- Nitrogen
oxides
- Carbon
monoxide
- Opacity
- Volatile
organic compounds
- Semivolatile
organic compounds
- Total
Hydrocarbons
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- Hydrogen
chloride
- Dioxins
/ furans
- Ammonia
- Mercury
- Selenium
- Silver
- Zinc
- Arsenic
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- Beryllium
- Cadmium
- Chromium
- Iron
- Lead
- Manganese
- Nickel
- Barium
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